Confidential Survey of GasGun™ Customers

J Integral has compiled a database, Table B, of all the GasGun applications performed prior to July 2003. In this data, names of operators, lease names, and well locations are confidential. The wells in Table A are duplicated in Table B. Although the individual well data in Table B is not as complete as the data in Table A, it is included to illustrate the range of applications and results of the tool.

Date Length (feet) Open or Cased Depth Formation County State Improved? comments
02/02/01 10 c 4854 Mississippi Barber KS n Recompletion, drinking fluid, shot w/ 300' fluid, no help.
02/02/01 4 c 4835 Cherokee Barber KS   New zone, see above.
10/23/01 4 c 3626 Douglas Barber KS n No help.
10/24/01 4 c 3626 Douglas Barber KS n  
12/13/01 2 c 4798 Mississippi Barber KS y  
07/17/02 4 c 2808 Tarkio Barber KS    
06/09/03 12 c 4820 Mississippi Barber KS    
06/18/03 4 c 4478 Mississippi Barber KS    
07/28/00 2 o 3287 Arbuckle Barton KS n 28 BOPD prior production dropped to zero.
04/23/01 4 c 3510 Arbuckle Barton KS    
09/17/01 6 c 3433 Arbuckle Barton KS y 1 BOPD > 6 BOPD
11/02/01 8 o 3566 Arbuckle Barton KS y Operator says made more water and oil, but wasn't specific.
11/28/01 6 c 3596 Arbuckle Barton KS w  
03/29/02 8 o 3342 Arbuckle Barton KS    
12/17/02 10 c 3367 Arbuckle Barton KS   3.3BOPD>?
06/10/03 4 o 3257 Arbuckle Barton KS    
06/26/03 6 o 3452 Arbuckle Barton KS    
09/27/00 6 c 2467 Simpson Butler KS y Some help, initally, later fraced at 1000 psi rather than 2200 psi experienced in neighboring well.
10/16/00 8 o 2418 Arbuckle Butler KS   Been sitting 1wk, Fluid level @2100'.
10/16/00 8 c 2478 Arbuckle Butler KS   New well, lost 100' of 5/16" wireline.
10/19/00 8 o 2394 Arbuckle Butler KS y One of these three Arbuckle wells, 7 BOPD, 20 BWPD, holding much better than when acidized only, acidized later at lower pressure.
04/17/01 6 o 2421 Arbuckle Butler KS y Cased hole gun shot in open hole, shot 1' off bottom, wireline stuck, cut wire 10' from tool ($2K-$3K), testing for large field, previous results good, acid jobs of 100 and 300 gallons, went on vacuum and did not produce water.
04/18/01 10 o 2384 Arbuckle Butler KS y On 8/3/01 report, 3 success, 8.7>30 BOPD, one went to water, 2 still unknown but not water.
04/18/01 6 c 2360 Arbuckle Butler KS y  
04/18/01 4 c 2447 Arbuckle Butler KS n  
04/21/01 6 c 2341 Arbuckle Butler KS y Heard from Log Tech that one of these wells later came in at 12 BOPD and is holding at 12 BOPD.
04/21/01 10 o 2369 Arbuckle Butler KS    
10/11/01 2 o 2456 Arbuckle Butler KS    
12/13/01 10 o 2377 Arbuckle Butler KS y 2 BOPD, 14 BWPD after gun 6-8 BOPD & 20BWPD.
12/13/01 4 o 2364 Arbuckle Butler KS y 2 BOPD, 20 BWPD after gun 6-8 BOPD & 30 BWPD.
12/13/01 10 c 2398 Arbuckle Butler KS y Making 6 BOPD but now getting chunks from previous polymer treatment, needs to do fair amount of rework to well.
12/13/01 4 c 2392 Arbuckle Butler KS w 3 BOPD, 14 BWPD well broke into "lots" of water.
12/21/01 8 c 2337 Arbuckle Butler KS y Log Tech says 25 BOPD levelling at 15.
01/08/02 10 o 2240 Arbuckle Butler KS    
01/03/02 4 c 2513 Mississippi Butler KS y 1 BOPD > 2.8 BOPD, increased water by greater factor but not a problem for customer.
02/25/02 6 o 2328 Arbuckle Butler KS    
05/07/02 10 c 2398 Arbuckle Butler KS y Well had polymer treatment in 80's to shut off water but shut off production too, came in at 6 BOPD and 30 BWPD after gun, customer happy.
06/07/02 8 c 2366 Arbuckle Butler KS y Only 1/2 BOPD better than before, is going to P&A.
08/05/02 4 o 2617 Arbuckle Butler KS n Arbuckle was producing water, shut off with squeeze, shot gun and got nothing.
08/15/02 4 c 2342 Arbuckle Butler KS y 1> 7 BOPD after acid
09/03/02 2 c 2570 Simpson Butler KS y Can't normally frac or brings in water, shot gun but no initial improvement, was later able to do small frac and got 7 BOPD & 4 BWPD, customer happy.
10/17/02 10 o 2447 Arbuckle Butler KS y 3>28BOPD, 60>171BWPD.
10/17/02 10 o 2439 Arbuckle Butler KS   2>? BOPD, 35>? BWPD.
12/17/02 2 c 2398 Arbuckle Butler KS n 1BOPD>?, 6BWPD>now just making all water.
02/12/03 4 c 2451 Arbuckle Butler KS    
04/08/03 16 c 2503 Arbuckle Butler KS    
04/15/03 4 c 2538 Arbuckle Butler KS y 2BOPD>4BOPD with Acid treatment.
04/15/03 2 c 2529 Arbuckle Butler KS y 2BOPD>4BOPD with Acid treatment.
05/29/03 2 c 2472 Arbuckle Butler KS   Cased hole gun shot in open hole.
05/29/03 6 c 2445   Butler KS    
06/02/03 10 o 2429 Arbuckle Butler KS    
06/12/03 4 c 2564 Arbuckle Butler KS    
07/16/03 10 o 2448 Arbuckle Butler KS    
12/03/01 10 c 1972 Mississippi Chautauqua KS y Log Tech says it increased and was acidized.
12/03/01 6 c 1659 Mulky Chautauqua KS y Coal, gas increased enough to run pumps.
01/15/02 6 c 1588 Mulky Chautauqua KS   Left 600' of line in hole, 1/23 fished line, cable head and top of tool came out inverted, obstruction at 800'.
01/15/02 6 c 1706 Mulky Chautauqua KS   Left 1300' of line in hole, fished out and cleared gun to bottom.
04/11/02 4 c 1914 Riverton Coal Chautauqua KS y Perforated 8 SPF > making more gas.
04/11/02 6 c 1972 Mississippi Chautauqua KS y Perforated 8 SPF > making more gas.
04/11/02 6 c 2011 Mississippi Chautauqua KS    
04/11/02 6 o 1802 Mississippi Chautauqua KS    
01/05/01 10 c 1477 Bartellsville Coffey KS   New well, making lots of water on 1/18, will continue to pump.
09/14/00 8 c 5035 Pawnee Comanche KS y 5 1/2" Casing, 70 > 140 MCF/D 0? > 3 BOPD, improving.
09/14/00 4 c 5143 Mississippi Comanche KS y 5 1/2" Casing, 70 > 140 MCF/D 0? > 3 BOPD, improving .
09/27/00 8 c 4974 Altamont Comanche KS   Lost 650' of line.
09/27/00 8 c 5024 Pawnee Comanche KS    
09/25/00 6 c 5070 Mississippi Comanche KS    
10/04/00 8 c 5020   Comanche KS    
10/04/00 6 c 5130   Comanche KS    
11/09/00 6 c 5342 Mississippi Comanche KS    
02/14/01 6 c 5080 Mississippi Comanche KS   New well, tight hole well.
04/10/01 6 c 5163 Ft. Scott Comanche KS   4 shots/ft, acidized, squeezed, 6 shots/ft, then GasGun.
04/12/01 6 c 5163 Ft. Scott Comanche KS   Second shot in exact same spot.
01/28/02 6 c 5154   Comanche KS    
09/17/02 4 c 3538 Stotler Lime Comanche KS    
01/09/03 4 c 5821 Viola Comanche KS    
01/30/03 4 c 5838 Viola Comanche KS    
01/30/03 4 c 5824 Viola Comanche KS    
01/30/03 6 c n/a Mississippi Comanche KS    
03/10/03 12 c 5330 Mississippi Comanche KS    
05/12/03 4 c 4980 Mississippi Comanche KS   Somewhat stuck, cleared 20' wire and later rubber with junk basket, used as prefrac, went to water, squeeze.
05/12/03 10 c 4948 Mississippi Comanche KS   see above
05/13/03 8 c 5592   Comanche KS   Bailed down to 2592' of fluid.
10/30/01 4 c 2983 Mississippi Cowley KS y #NAME?
02/12/02 4 c 3342   Cowley KS   1.67 BOPD>
04/01/02 4 c 2358 Layton Cowley KS    
04/04/02 4 c 3062   Cowley KS   Report of rubber getting in pump
05/06/02 10 c 3090 Mississippi Cowley KS   Pulling out rubber with swab, marble size up to a 3.5" - 11" piece
10/01/02 4 c 3464   Decatur KS    
11/06/00 4 o 3400 Arbuckle Ellis KS n No help, been shut down for 15 years, acidized after shot and brought in the ocean.
04/01/02 4 c 3600 Kansas City Ellis KS y Brought back entire canister, acid job went with 850 psi rather than usual 1600, 3 BOPD > 14 BOPD for month steadied at 8 BOPD.
07/23/02 6 c 3279 Kansas City Ellis KS    
08/01/02 4 o 3387 Arbuckle Ellis KS    
10/09/02 8 c 3640 Arbuckle Ellis KS    
10/17/02 4 c 3388   Ellis KS    
10/17/02 4 c 3582 Arbuckle Ellis KS    
10/16/02 4 c 3569   Ellis KS   New well
07/08/03 2 c 3412 Arbuckle Ellis KS   Shot in open hole
07/08/03 2 c 3396 Arbuckle Ellis KS   Shot in open hole
04/19/02 4 o 3295 Arbuckle Ellsworth KS    
05/29/02 8 c 3390   Ellsworth KS   Existing production 1 BOPD
08/19/02 6 o 3234 Arbuckle Ellsworth KS    
02/25/02 4 c 4250 Mississippi Finney KS    
05/06/02 10 c 650   Franklin KS   1/4 BOPD before shot, added section of tubing to bottom of gun and ran in easily, lost 250ft of line and had to fish.
05/22/02 4 c 3662 Regan Sand Graham KS    
11/11/02 4 c 3578   Graham KS    
02/02/01 6 c 4373 Mississippi Harper KS   New completion.
12/18/01 4 c 4448 Mississippi Harper KS y New gas well, 4.5" casing, 0.48" @6spf, acidized and wants to try to put on prod. w/out frac., initial prod. Is 340 MCF in 4 hours.
12/26/01 4 c 4420 Mississippi Harper KS y New gas well, 4.5" casing, 0.48" @6spf, acidized and fraced, treating pressure normaly 1,900psi, after GasGun treating pressure 1,000psi.
10/18/02 6 c 4501 Mississippi Harper KS   Gas well
11/07/02 4 o 4320   Harper KS    
06/17/03 6 c 4434 Mississippi Harper KS    
06/23/03 6 c 4417 Mississippi Harper KS    
11/28/01 4 c 2912 Mississippi Harvey KS n Previously had small show of gas that could light on fire, hole went dry after shot.
11/27/02 8 c 3236 Mississippi Harvey KS   Cased hole guns shot in open hole
08/21/01 6 c 4274 Mississippi Hodgeman KS y Cased hole gun shot in open hole, 1.67 > 16.7 BOPD and 20 > 85 BWPD for 2 weeks.
10/16/01 8 c 4422 Mississippi Hodgeman KS n No help.
02/20/02 4 c 4053 Mississippi Kingman KS   Casing split, 3718-3745.
03/13/02 6 c 4125 Mississippi Kingman KS n Shot in open hole, had to drop fluid on top to get going, 7' of open hole, 3900' fluid, dragged and broke off 15' of line 500' unchanged - disappointed.
05/16/03 6 c 4372 Mississippi Kingman KS y Gas well went from 30 MCF > 68 MCF
05/21/03 4 c 1714 Indian Cave Kingman KS    
01/14/03 6 c 1431 Burgess Leavenworth KS    
06/30/03 4 c 1470 Mississippi Leavenworth KS    
06/30/03 26 c 1396 McLouth Leavenworth KS    
07/22/03 10 c n/a McLouth Leavenworth KS    
07/22/03 6 c " McLouth Leavenworth KS    
05/21/02 8 c 2962 Mississippi McPherson KS    
02/12/02 10 c 5796 Chester Meade KS    
08/30/02 4 c 1306 coal Montgomery KS y Increase of only 1-2 MCFPD and no increase in water
08/30/02 4 c 1463 coal Montgomery KS n No help
06/04/02 4 c 1044 Riverton Coal Neosho KS n Had been fraced several times, customer said not very good candidate, plan to do more.
11/09/01 2 c 4305   Ness KS    
12/10/01 4 c 4248 Cherokee Ness KS    
04/29/02 10 o 3674 Arbuckle Norton KS y 3.8 > 6.8 BOPD (Log Tech says it was 1.8 originally)
03/13/01 8 c 1390 Burgess Osage KS   Log Tech does not hold much hope for this well.I205
03/13/01 8 c 5430 Mississippi Osage KS    
02/19/02 10 c 3208   Osborne KS    
06/13/01 4 o 4355 Mississippi Pawnee KS y Old well, 1.67 BOPD > 2.42, is going back to treat with carbon disulfide and acid like 4 wells done after this one.
08/16/01 6 o 4319 Mississippi Pawnee KS   These three wells are in chert.
09/11/01 6 c 4356 Mississippi Pawnee KS    
12/28/01 10 c 2446   Pawnee KS n New well, Log Tech and customer feel there wasn't anything there, acid treatment also didn't help.
12/28/01 8 c 2254   Pawnee KS n -ditto-
04/22/02 6 c 2133 Krider Pawnee KS    
06/05/02 10 o 4095 Conglomerate Pawnee KS    
07/03/02 6 c 3862 Simpson Pawnee KS    
07/23/02 6 c 1911   Pawnee KS    
09/17/01 4 c 4108 Cherokee Pratt KS   "Went on vacuum"
04/03/02 4 c 3662 Viola Reno KS   Lost 6' line.
09/28/01 4 c 2986 Stranger Sand Rice KS    
06/11/02 4 o 3218   Rice KS    
06/21/02 4 c 3275 Misener Rice KS   Cased hole gun shot in open hole, used pre-frac.
09/06/02 4 c 3302   Rice KS    
11/13/02 4 c 3215 Conglomerate Rice KS    
01/17/03 2 c 3273 Arbuckle Rice KS   Cased hole gun shot in open hole.
06/16/03 4 o 3255 Arbuckle Rice KS    
11/07/01 6 c 1764 Hunton Riley KS y Doubled production.
12/02/02 6 c 3051 Kansas City Rooks KS   Lost 400' of line in hole.
08/23/01 4 o 4413 Mississippi Rush KS y Wells shares storage tank, total volume from 30 > 80,
                estimate 10 BOPD increase from GasGun.
09/24/01 6 c 4392 Mississippi Rush KS   Shot 2' of GasGun in cased hole and remaining 4 " in open hole.
10/01/01 6 c 4364 Mississippi Rush KS    
01/23/01 4 c 2393 Tarkio Russell KS y Lost cable head, recompletion, shot above bridge plug, 0>5 BOPD and lots of gas (can't sell and is gas locking), customer pleased, still at 5 BOPD after 8 months.I236
01/23/01 4 c 2385 Tarkio Russell KS y see above
11/30/01 6 c 3214 Arbuckle Russell KS    
01/24/02 2 c 3321 Arbuckle Russell KS   2BOPD>?
02/07/02 2 c 2839 Kansas City Russell KS    
02/07/02 4 c 2742 Kansas City Russell KS    
04/11/02 4 c 2955 Topeka Russell KS y  
04/11/02 4 c 2944 Topeka Russell KS y Producing 1.5 BOPD before shot > 6 BOPD
05/31/02 2 c 3322 Arbuckle Russell KS    
03/13/03 4 o 3990 Mississippi Sedgwick KS    
04/10/02 6 c 3399   Seward KS y Mostly water increase, but pleased and will shoot more.
05/07/02 6 c 5714 Chester Seward KS   Followed GasGuns with acid frac.
05/07/02 8 c 5700 Chester Seward KS    
05/10/02 20 c 5764 Chester Seward KS   Followed GasGuns with acid frac.
08/14/02 4 c 2029   Sherman KS   New well.
10/04/01 6 c 3520 Arbuckle Stafford KS n Well went to water, operator not unhappy.
11/08/01 8 o 3447 Arbuckle Stafford KS y 1 BOPD increase over previous production.
11/13/01 6 c 3502 Arbuckle Stafford KS y 1 BOPD increase over previous production.
01/23/02 10 c 3360 Arbuckle Stafford KS   Lost 250' line, 5BOPD>?
04/01/02 10 c 3352 Arbuckle Stafford KS    
07/01/02 2 c 3479 Kansas City Stafford KS    
08/19/02 4 c 3739 Arbuckle Stafford KS    
11/14/02 8 o 3265 Arbuckle Stafford KS    
12/12/01 4 c 6242   Stevens KS    
12/12/01 8 c 6228   Stevens KS   Got stuck, suspect casing damage?
12/27/02 16 c 5495 Mississippi Stevens KS y Previous acid job didn't work treating pressure 2000psi after GasGun treating pressure 1000psi.I262
03/13/02 6 c 3511   Sumner KS    
06/24/02 6 c 3340 Mississippi Sumner KS    
08/08/02 2 c n/a   Sumner KS    
06/18/03 4 c 2986 Stallnaker Sumner KS    
03/05/02 10 c 3809 Marmiton Trego KS    
07/09/02 6 c 4128 Cherokee Trego KS    
07/09/02 2 c 4148 Cherokee Trego KS    
05/07/02 16 c 946   Wallace KS    
06/25/02 6 o 3255 Arbuckle   KS   30 BWPD, 1 BOPD>?
10/30/02 6 c n/a     KS   Cased hole gun shot in open hole, 2>? BOPD.I35

Table B Applications of Gasgun in Kansas


References

1) Schmidt, R. A., Boade, R. R., and Bass, R. C., "A New Perspective on Well Shooting - Behavior of Deeply Buried Explosions and Deflagrations," Journal of Petroleum Technology, Vol., 33, No. 7, pp. 1305-1311, July 1981.

2) Schmidt, R. A., Warpinski, N. R., Finley, S. J., and Shear, R. C., "Multi-Frac Test Series Final Report," Sandia Laboratories Report, SAND81-1239, Albuquerque, New Mexico, November 1981.

3) Schmidt, R. A., Warpinski, N. R., and Cooper, P. W., "In Situ Evaluation of Several Tailored-Pulse Well-Shooting Concepts," Proceedings of 1980 SPE/DOE Symposium on Unconventional Gas Recovery, Pittsburgh, Pennsylvania, SPE 8934, May 1980.

Wells

Well
Formation
Kansas County
Vess Oil Corp.; Hamilton ‘A’ #4 Arbuckle Butler
Vess Oil Corp. Waterhouse #1 Mississippian Limestone Hodgeman
Vess Oil Corp.; Oliver #4 Mississippian Limestone Pawnee
Vess Oil Corp.; John Nolte #2 Arbuckle and Lansing-KansasCity D, F, I, J & K zones Stafford
Vess Oil Corp.; Hewitt #2 Arbuckle Stafford
Vess Oil Corp.; Bauer-Nolte #4 Arbuckle and Lansing-Kansas City F & J zones Stafford
Vess Oil Corp.; Lyda #2 Arbuckle Barton
Vess Oil Corp.; Wells Unit #29-3 Mississippian Limestone Rush
Vess Oil Corp.; McJunkin #1 Mississippian Limestone Rush
Vess Oil Corp.; Ryan ‘P’ #1 Mississippian Limestone Rush

URL: http://www.nmcpttc.org/Case_Studies/Gasgun/confidentialsurvey.html
Updated February 2003